Display title | Engineering:Crew Dragon In-Flight Abort Test |
Default sort key | Crew Dragon In-Flight Abort Test |
Page length (in bytes) | 18,294 |
Namespace ID | 3034 |
Namespace | Engineering |
Page ID | 263449 |
Page content language | en - English |
Page content model | wikitext |
Indexing by robots | Allowed |
Number of redirects to this page | 0 |
Counted as a content page | Yes |
Page image |  |
HandWiki item ID | None |
Edit | Allow all users (infinite) |
Move | Allow all users (infinite) |
Page creator | imported>Jport |
Date of page creation | 15:09, 4 February 2024 |
Latest editor | imported>Jport |
Date of latest edit | 15:09, 4 February 2024 |
Total number of edits | 1 |
Recent number of edits (within past 90 days) | 0 |
Recent number of distinct authors | 0 |
Description | Content |
Article description: (description ) This attribute controls the content of the description and og:description elements. | SpaceX Crew Dragon In-Flight Abort Test (also known as Crew Dragon Launch Escape Demonstration) was a successful test of the SpaceX Dragon 2 abort system, conducted on 19 January 2020. It was the final assessment for the Crew Dragon capsule and Falcon 9 launch system before they would be certified to... |